KrZy8 Hissy Fit - KeyBoard Techs Needed!
Posted: Wed Nov 25, 2020 10:09 pm
Well, here we go again. KrZy8 throwing a hissy fit.
Running rough / stalling off idle. 32-35 mpg not high 30's low 40's as baseline. Unfortunately, KrZy8 sat for too long while I was away working.. ~ 3 months total.
Troubleshooting Plan
Check Compression
COLD 1=190 2=190 3=175 4=175 7.9% delta. Note.. I used a throttle lock.. and think it slipped at #3, 4 reading, closing the butterflys somewhat. Will test later.
Check Air Filter for mice nest
Clean. Air filter kinda dirty but not excessively bad. Replaced.
Check/Replace injectors
Had 4 refurbished RC Engineering from 2017 sitting in the spares box. Tested each using 9 vDc battery. 3 of 4 not clicking. Used a home made test fixture to supply gasoline under slight pressure to injector, whacked them with screw driver, and each then clicked and sprayed like a male cat.
Replace fuel in tank with fresh
Thinking some condensation might have formed.. and I use SeaFoam, which FortNine recently demonstated is not the best storage solution.
On the lift, KrZy8 is crisp, GREAT. Fast throttle response.. Snappy!
So that's it for now. Now let's go ride..
---------
Good news, bad news
Good news - Ran great for first 50 miles or so.. Snappy, high 30's mpg, STRONG
Bad news - Instantly... KaBoom, dropped a cylinder or so it seems. Exhaust rough, has the hollow sound of a cylinder not firing. WTFO? Decided to take 'main' roads home for easier tow truck access should it come to that.
MPG's now in low 30's high 20's.
Idles fine. But under load, missing, and very noticeably.
Then, MAGIC and instantly, running purrfect and MPG's climb to mid 40's. Oh Happy Day.
Then, BAM, and back to crapola.
What can it be?
Sticky fuel injector?
Water blob in tank, sloshing around, getting picked up once in awhile when cornering or whatever?
Ignition coils? (Idle is fine, throttle under no load fine, but under load missing... higher compression blowing spark out?) BTW, coils, leads, caps replaced with used eBay units 2019-08-10.
Spark plug going south?
Fuel pp failing (I can put the 2013 tank of the 2006 to test!)
Unfortunately, no auto store in Paso Robles or Atascadero has qty 4 CR8EIX NGK plugs.. Decide to soilder on to Paso, pick up 3 NGK's then to Atascadero for some fancy smancy E3 plug.. just for testing.
Current plan
Replace sparking plugs
Check battery connections + ground (even though starting and charging is working fine)
Pull and test FI's on bench with 9vdc battery and test rig
Re-run compression check when warm and known TB's fully open
Truly dissapointing but so it goes.
HOPEFULLY I'll find something really stupid I did.. like not fully connecting a FI connector or likewise..
Turkey day tomorrow.. but maybe I can get to the shop and play. KrZy8 already on the lift.
SO WHAT DO YOU FART SMELLERS SUGGEST?
Running rough / stalling off idle. 32-35 mpg not high 30's low 40's as baseline. Unfortunately, KrZy8 sat for too long while I was away working.. ~ 3 months total.
Troubleshooting Plan
Check Compression
COLD 1=190 2=190 3=175 4=175 7.9% delta. Note.. I used a throttle lock.. and think it slipped at #3, 4 reading, closing the butterflys somewhat. Will test later.
Check Air Filter for mice nest
Clean. Air filter kinda dirty but not excessively bad. Replaced.
Check/Replace injectors
Had 4 refurbished RC Engineering from 2017 sitting in the spares box. Tested each using 9 vDc battery. 3 of 4 not clicking. Used a home made test fixture to supply gasoline under slight pressure to injector, whacked them with screw driver, and each then clicked and sprayed like a male cat.
Replace fuel in tank with fresh
Thinking some condensation might have formed.. and I use SeaFoam, which FortNine recently demonstated is not the best storage solution.
On the lift, KrZy8 is crisp, GREAT. Fast throttle response.. Snappy!
So that's it for now. Now let's go ride..
---------
Good news, bad news
Good news - Ran great for first 50 miles or so.. Snappy, high 30's mpg, STRONG
Bad news - Instantly... KaBoom, dropped a cylinder or so it seems. Exhaust rough, has the hollow sound of a cylinder not firing. WTFO? Decided to take 'main' roads home for easier tow truck access should it come to that.
MPG's now in low 30's high 20's.
Idles fine. But under load, missing, and very noticeably.
Then, MAGIC and instantly, running purrfect and MPG's climb to mid 40's. Oh Happy Day.
Then, BAM, and back to crapola.
What can it be?
Sticky fuel injector?
Water blob in tank, sloshing around, getting picked up once in awhile when cornering or whatever?
Ignition coils? (Idle is fine, throttle under no load fine, but under load missing... higher compression blowing spark out?) BTW, coils, leads, caps replaced with used eBay units 2019-08-10.
Spark plug going south?
Fuel pp failing (I can put the 2013 tank of the 2006 to test!)
Unfortunately, no auto store in Paso Robles or Atascadero has qty 4 CR8EIX NGK plugs.. Decide to soilder on to Paso, pick up 3 NGK's then to Atascadero for some fancy smancy E3 plug.. just for testing.
Current plan
Replace sparking plugs
Check battery connections + ground (even though starting and charging is working fine)
Pull and test FI's on bench with 9vdc battery and test rig
Re-run compression check when warm and known TB's fully open
Truly dissapointing but so it goes.
HOPEFULLY I'll find something really stupid I did.. like not fully connecting a FI connector or likewise..
Turkey day tomorrow.. but maybe I can get to the shop and play. KrZy8 already on the lift.
SO WHAT DO YOU FART SMELLERS SUGGEST?